Tìm Kiếm

  • Report
    Report

    Jul 1, 2019 ... Attachment IV Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 24, 2019 Pressure Safety Valve Malfunction in the TKC Unit ...

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    (1 Mb PDF, 5 pgs)

    Jul 1, 2019 ... Attachment IV Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 24, 2019 Pressure Safety Valve Malfunction in the TKC Unit ...

  • Report
    Report

    Jul 9, 2019 ... Attachment II Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 5, 2019 - April 12, 2019 Start-up and Commissioning of Hydrogen Plant Train 2 (S-4450) ...

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    (1 Mb PDF, 5 pgs)

    Jul 9, 2019 ... Attachment II Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 5, 2019 - April 12, 2019 Start-up and Commissioning of Hydrogen Plant Train 2 (S-4450) ...

  • Report
    Report

    Thg12 2, 2022 ... Attachment V Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events September 16, 2022 Flaring Due to Incorrect Logic on Safety Instrumented System ...

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    (188 Kb PDF, 5 pgs)

    Thg12 2, 2022 ... Attachment V Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events September 16, 2022 Flaring Due to Incorrect Logic on Safety Instrumented System ...

  • Report
    Report

    Thg6 7, 2022 ... Attachment I Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 4, 2022 Flaring Due to Process Upset in Amine Scrubber ...

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    (213 Kb PDF, 5 pgs)

    Thg6 7, 2022 ... Attachment I Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 4, 2022 Flaring Due to Process Upset in Amine Scrubber ...

  • Report
    Report

    Thg10 7, 2022 ... ...

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    (795 Kb PDF, 4 pgs)

    Thg10 7, 2022 ... ...

  • Report
    Report

    Thg4 13, 2022 ... Attachment I Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 25, 2022 Flaring Due to Safety System Activation ...

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    (190 Kb PDF, 5 pgs)

    Thg4 13, 2022 ... Attachment I Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 25, 2022 Flaring Due to Safety System Activation ...

  • Report
    Report

    Thg10 18, 2022 ... ...

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    (5 Mb PDF, 5 pgs)

    Thg10 18, 2022 ... ...

  • Report
    Report

    Thg6 16, 2020 ... ...

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    (106 Kb PDF, 3 pgs)

    Thg6 16, 2020 ... ...

  • Report
    Report

    Jun 16, 2020 ... ...

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    (130 Kb PDF, 3 pgs)

    Jun 16, 2020 ... ...

  • Report
    Report

    Thg4 12, 2023 ... Regulation 12 Rule 12 Reportable Flaring Event Causal Analysis Report 1. Report Date: March 10, 2023 2. Refinery Name and Site Number: Martinez Refining Company - BAAQMD Site # A0011 3. Refinery ...

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    (154 Kb PDF, 5 pgs)

    Thg4 12, 2023 ... Regulation 12 Rule 12 Reportable Flaring Event Causal Analysis Report 1. Report Date: March 10, 2023 2. Refinery Name and Site Number: Martinez Refining Company - BAAQMD Site # A0011 3. Refinery ...

  • Report
    Report

    Thg6 14, 2023 ... Attachment VI Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 10 - 11, 2023 Flaring Due to Startup of Hydrogen Plant Train 2 May 30, ...

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    (174 Kb PDF, 4 pgs)

    Thg6 14, 2023 ... Attachment VI Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 10 - 11, 2023 Flaring Due to Startup of Hydrogen Plant Train 2 May 30, ...

  • Report
    Report

    Nov 18, 2025 ... BAAQMD received on 11/18/25 Kris Battleson HSE Manager, Richmond Refinery November 18, 2025 Via E-mail Bay Area Air District Attn: Compliance and Enforcement Division 375 Beale Street, Suite ...

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    (286 Kb PDF, 5 pgs)

    Nov 18, 2025 ... BAAQMD received on 11/18/25 Kris Battleson HSE Manager, Richmond Refinery November 18, 2025 Via E-mail Bay Area Air District Attn: Compliance and Enforcement Division 375 Beale Street, Suite ...

  • Report
    Report

    Sep 14, 2023 ... FLARE CAUSAL ANALYSIS REPORT 1) Date on which the report was drafted. August 15, 2023 2) The refinery name and site number. Tesoro Martinez Refinery, Plant # B2758, wholly owned subsidiary of ...

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    (459 Kb PDF, 4 pgs)

    Sep 14, 2023 ... FLARE CAUSAL ANALYSIS REPORT 1) Date on which the report was drafted. August 15, 2023 2) The refinery name and site number. Tesoro Martinez Refinery, Plant # B2758, wholly owned subsidiary of ...

  • Report
    Report

    Thg6 14, 2023 ... Attachment VII Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 12-13, 2023 Flaring Due to Startup of Hydrogen Plant Train 2 May 30, ...

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    (174 Kb PDF, 4 pgs)

    Thg6 14, 2023 ... Attachment VII Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events March 12-13, 2023 Flaring Due to Startup of Hydrogen Plant Train 2 May 30, ...

  • Report
    Report

    Feb 15, 2024 ... BAAQMD received 01/26/24 Attachment VI Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events November 28, 2023 Flaring Due to Startup of Hydrogen Plant Train ...

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    (289 Kb PDF, 4 pgs)

    Feb 15, 2024 ... BAAQMD received 01/26/24 Attachment VI Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events November 28, 2023 Flaring Due to Startup of Hydrogen Plant Train ...

  • Report
    Report

    Nov 25, 2025 ... BAAQMD received on 11/25/25 Via Email Notification November 25, 2025 Reportable Flaring Event Causal Analysis September 11, 2025 Plant No. B2626 Dr. Philip Fine Bay Area Air District Bay Area ...

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    (315 Kb PDF, 5 pgs)

    Nov 25, 2025 ... BAAQMD received on 11/25/25 Via Email Notification November 25, 2025 Reportable Flaring Event Causal Analysis September 11, 2025 Plant No. B2626 Dr. Philip Fine Bay Area Air District Bay Area ...

  • Report
    Report

    Thg4 29, 2025 ... BAAQMD received on 4/28/25 Attachment II Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 2, 2025 Flaring Due to Failure of a Condensate Drum Level Indicator ...

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    (320 Kb PDF, 5 pgs)

    Thg4 29, 2025 ... BAAQMD received on 4/28/25 Attachment II Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 2, 2025 Flaring Due to Failure of a Condensate Drum Level Indicator ...

  • Report
    Report

    Thg4 29, 2025 ... BAAQMD received on 4/28/25 Attachment III Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 07, 2025 Flaring Due to Startup of Hydrogen Plant Trains ...

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    (186 Kb PDF, 4 pgs)

    Thg4 29, 2025 ... BAAQMD received on 4/28/25 Attachment III Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events February 07, 2025 Flaring Due to Startup of Hydrogen Plant Trains ...

  • Report
    Report

    Oct 28, 2025 ... BAAQMD received on 10/29/25 Kris Battleson HSE Manager, Richmond Refinery October 28, 2025 Via E-mail Bay Area Air District Attn: Compliance and Enforcement Division 375 Beale Street, Suite 600 ...

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    (305 Kb PDF, 6 pgs)

    Oct 28, 2025 ... BAAQMD received on 10/29/25 Kris Battleson HSE Manager, Richmond Refinery October 28, 2025 Via E-mail Bay Area Air District Attn: Compliance and Enforcement Division 375 Beale Street, Suite 600 ...

  • Report
    Report

    Feb 15, 2024 ... BAAQMD received 01/26/24 Attachment V Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events November 27, 2023 Flaring Due to Shutdown of Hydrogen Plant Trains ...

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    (289 Kb PDF, 4 pgs)

    Feb 15, 2024 ... BAAQMD received 01/26/24 Attachment V Causal Analysis Report Chevron Richmond Refinery Reportable Flaring Events November 27, 2023 Flaring Due to Shutdown of Hydrogen Plant Trains ...

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Cập Nhật Lần Cuối: 08/11/2016